 
          2793
        
        
          Technical Committee 212 /
        
        
          
            Comité technique 212
          
        
        
          with granular material were fully saturated leading to extreme
        
        
          softening (swelling) of the clay in the base of the excavations.
        
        
          A total of five ~10m deep CPTs were used to characterise
        
        
          the site and backfill. Using a N
        
        
          kt
        
        
          = 20 (Butcher et al. 2009) the
        
        
          variation of s
        
        
          u
        
        
          and density (γ) of the London clay below 3m (the
        
        
          founding plane) corroborates with previous observations. A
        
        
          profile from Footing 5 is shown in Figure 2.
        
        
          Figure 2. CPT profile of Footing 5
        
        
          2.3
        
        
          
            Load schedule
          
        
        
          The footings tests were carried out over a period of six working
        
        
          days (18
        
        
          th
        
        
          - 25
        
        
          th
        
        
          July 2012). Table 3.2 shows the order with
        
        
          which the tests were carried out. The small displacement tests
        
        
          (denoted ‘A’) of Footings 2 and 3 examined the rate effect at
        
        
          small displacements in the fully bonded and breakaway
        
        
          conditions.  The first load test on Footing 4 was a design test to
        
        
          BS EN61773:1997 (BSI 1997).
        
        
          The load was applied to the footing stubs using a hydraulic
        
        
          jack system. The setup of the reaction beams and jack is shown
        
        
          in Figure 3. The reaction beams at the base were orientated
        
        
          parallel to the line of the excavations and outside the failure
        
        
          zone of a 30
        
        
          o
        
        
          frustum. The cross beams with the hydraulic jack
        
        
          were inclined so that the footings could be pulled up in line with
        
        
          the footing chimney. Wedges were placed under the cross beam
        
        
          to achieve the required rake angles. The hydraulic ram had a
        
        
          total stroke length of 150mm (w/B=10%).
        
        
          The resistance of the footing during uplift was measured
        
        
          using a load cell mounted above the hydraulic jack. The
        
        
          displacement of the footing was measured by mounting LVDTs
        
        
          on a reference beam. The LVDTs were vertically orientated and
        
        
          recorded the movement from the head of the chimney. The data
        
        
          from the instrumentation was acquired using a Campbell
        
        
          CR5000 data logger sampling at 10-100s/s.
        
        
          3 FIELD TEST RESULTS
        
        
          3.1
        
        
          
            Load-displacement behavior
          
        
        
          The load-displacement profiles of the tests conducted with a
        
        
          London clay base displayed an extremely stiff response (see
        
        
          Test 1-A and 5-A.
        
        
          The loading rates during the first few millimetres of
        
        
          movement was in the range 276 kN/mm (Test 2-A) – 333
        
        
          kN/mm (Test 1-A). The peak capacities of the footings were
        
        
          achieved between w/B = 2.1 - 4.7% versus the secondary test
        
        
          which were generally in excess of 7%. Although the Tests 1-A,
        
        
          did not affect uplift capacity. The measured uplift capacities
        
        
          were similar for both tests (<10% difference) during the first
        
        
          10mm of uplift and at peak there is a difference of 50 kN versus
        
        
          Test 1-A and 5-A.
        
        
          Test 3-A was
        
        
          2-A and 5-A were conducted at different uplift velocities this
        
        
          used to examine the difference that base
        
        
          co
        
        
          gr
        
        
          Ta 2. Load schedule
        
        
          
            est
          
        
        
          
            w (mm)
          
        
        
          
            v
          
        
        
          
            f
          
        
        
          
            (mm/s)
          
        
        
          ntact conditions at small displacements would have. Although
        
        
          the test did not reach its peak the stiffness response is
        
        
          comparable with Footing 2-A. This implies that the base
        
        
          condition contribution was similar to the footings tested on
        
        
          London clay and that the blinding did not fulfill its purpose of
        
        
          excluding suctions from uplift i.e. acted a free draining material.
        
        
          Tests 3-B and 4-B indicated that the performance of Type 2
        
        
          anular fill is extremely poor and could only mobilise ~50% of
        
        
          Q
        
        
          des
        
        
          at w=10mm. Large displacements were required for the
        
        
          granular fill to mobilise sufficient strength to produce uplift
        
        
          capacities equivalent to Q
        
        
          des
        
        
          (w = 60mm Test 3-B and w =
        
        
          80mm Test 4-B). It should be noted on Test 5-A reached Q
        
        
          des
        
        
          within a 10mm displacement.
        
        
          Figure 3. Field test arrangement
        
        
          ble
        
        
          
            Footing
          
        
        
          
            T
          
        
        
          1
        
        
          1-A
        
        
          150
        
        
          35
        
        
          2
        
        
          2-A
        
        
          15
        
        
          5
        
        
          2
        
        
          2-B
        
        
          150
        
        
          15
        
        
          3
        
        
          3-A
        
        
          15
        
        
          15
        
        
          3
        
        
          3-B
        
        
          150
        
        
          10
        
        
          4
        
        
          4-A
        
        
          BS EN61773:1997
        
        
          4
        
        
          4-B
        
        
          150
        
        
          15
        
        
          5
        
        
          5-A
        
        
          150
        
        
          35
        
        
          Figure 4. Load-displacement results for rapid uplift footings