 
          2705
        
        
          Technical Committee 212 /
        
        
          
            Comité technique 212
          
        
        
          
            Proceedings of the 18
          
        
        
          
            th
          
        
        
          
            International Conference on Soil Mechanics and Geotechnical Engineering, Paris 2013
          
        
        
          At the same time the author was requested to conduct
        
        
          driveability predictions using wave equation analysis of piles
        
        
          (WEAP) to assess if the casings could be  used as driven piles.
        
        
          One of the main criteria of interest was whether the piles could
        
        
          be driven far enough into the soft rock to achieve the required
        
        
          tension resistance, which was a controlling aspect of the tripod
        
        
          foundation design. This appeared to be the case, and with a
        
        
          smaller hammer than was being used for the dynamic testing.
        
        
          Construction started on the East Abutment and, again,
        
        
          problems with the concrete quickly became obvious. CSL
        
        
          testing indicated a significant defect at 25m below the top.
        
        
          (Figure 6).  Drill cores were conducted to investigate and repair
        
        
          the problem zone.  Coring confirmed a zone of aggregate only
        
        
          with no cement - exactly as predicted by the CSL.  (Figure 7).
        
        
          Further attempts were made to improve the concrete but in
        
        
          every case problems were detected.  If anything the concrete
        
        
          problems got worse, both in size and significance. (Figure 8).
        
        
          Prior to the abandonment of socketed piles one further test
        
        
          was conducted on the last socketed abutment pile.  No access
        
        
          tubes had been cast in this pile so low strain axial sonic pile
        
        
          integrity testing using a Pile Integrity Tester
        
        
          ®
        
        
          (PIT) was
        
        
          conducted (Figure 9). No integrity problems were detected
        
        
          using this method. A very slight increase in velocity was
        
        
          detected at the top of the socket but this was attributed to the
        
        
          change in diameter from 900mm to 780mm.
        
        
          6 DRIVEN TEST PILE
        
        
          Soon after the WEAP analyses were conducted a third test pile
        
        
          was installed.  Again, this was positioned adjacent to the bridge
        
        
          location and was not to be incorporated into the contract works.
        
        
          The 900x20mm steel tube casing was modified by removing the
        
        
          bottom collar and installing a 900x50mm driving shoe of 0.8m
        
        
          length.  This third test pile was driven with a Junttan HHK9A
        
        
          hammer, which has a 9t ram.  The pile was driven through the
        
        
          gravels and cobbles and 12m into the soft rock at a final set of
        
        
          2.9mm/bl. A restrike test was conducted the next day using the
        
        
          Junttan HHK16A hammer, which has a 16t ram. The pile had
        
        
          "set-up" to such an extent the set had reduced to 1.3mm/bl
        
        
          despite the hammer being significantly larger than the hammer
        
        
          used to drive the pile.  The resistance demonstrated during the
        
        
          
            Figure 5 - PDA measurements Test Pile 2
          
        
        
          
            Figure 4 - CSL test results Test Pile 2
          
        
        
          
            Figure 7 - Core of East Abutment NW pile
          
        
        
          
            Figure 6 CSL test result East Abutment NW pile