 
          2704
        
        
          Proceedings of the 18
        
        
          th
        
        
          International Conference on Soil Mechanics and Geotechnical Engineering, Paris 2013
        
        
          
            Proceedings of the 18
          
        
        
          
            th
          
        
        
          
            International Conference on Soil Mechanics and Geotechnical Engineering, Paris 2013
          
        
        
          The piles were 900mm OD with 20mm wall thickness steel
        
        
          tubes with a concrete socket in the rock.  At this site the socket
        
        
          was 780mm diameter.  The concrete was to be continued into
        
        
          the pile a sufficient distance to transfer the load by
        
        
          steel/concrete bond - about 8m. The concrete was to be heavily
        
        
          reinforced owing to high tension loading, with ten clusters of
        
        
          three 36mm diameter bars.
        
        
          The contractor initially installed the casings with a large
        
        
          down-the-hole hammer.  This used a 940mm hammer
        
        
          positioned at the bottom of the excavation and powered by
        
        
          compressed air.  The hammer drags the casing behind it by
        
        
          engaging a collar at the bottom of the casing.  Upon reaching
        
        
          rock the hammer can disengage the casing and bore a socket.
        
        
          At this site the hammer was removed after reaching the rock
        
        
          and a 780mm rock-roller drill was used to drill the socket. The
        
        
          method was well known to the contractor and is reputed to have
        
        
          excellent production rates in hard ground.  However, at this site
        
        
          the gravels and cobbles were loose and saturated.  There was
        
        
          frequently insufficient resistance to start the hammer and it
        
        
          stalled frequently.
        
        
          Progress was slow and delays were
        
        
          extensive.
        
        
          Owing to the remote site concrete was produced by a mobile
        
        
          batch plant at the site but was otherwise unremarkable. The
        
        
          piles were concreted using a tremie pipe with the shaft full of
        
        
          water or drilling fluid.
        
        
          4
        
        
          SOCKETED TEST PILES
        
        
          The first pile constructed at the site was a test pile that was not
        
        
          to be incorporated into the bridge.  It was a vertical full sized
        
        
          pile. To provide for dynamic testing the socket concrete was
        
        
          extended to the top of the pile. The test gauges were initially
        
        
          attached to the concrete through "windows" in the steel tube and
        
        
          the pile was considered as a combined section.  The top of the
        
        
          steel tube was cut back 25mm below the top of concrete to
        
        
          ensure the hammer acted on the concrete.  A 19mm plywood
        
        
          cushion was used between the hammer and the pile.
        
        
          Other than the permanent casing there was nothing
        
        
          unusual about the dynamic testing.  Concreting  had been
        
        
          completed about 14days prior to the test.
        
        
          Very strange measurements were obtained initially, with
        
        
          almost no force measured in the concrete.  (Figure 2). In
        
        
          addition it was observed after several blows that the concrete in
        
        
          the "window" had moved down relative to the steel.
        
        
          The gauges were moved to the steel tube and again very
        
        
          strange measurements were obtained The only way the
        
        
          measurements made sense was to use the properties of the steel
        
        
          tube only and assume the concrete was not working as part of
        
        
          the pile.  (Figure 3).  The hammer was removed and it was
        
        
          noted the top was level with the steel. The hammer was indeed
        
        
          acting on the steel tube.
        
        
          The concrete between the pile top and the gauges must
        
        
          have crushed by up to 44mm, being the 25mm upstand of
        
        
          concrete plus the thickness of the pile cushion. The hammer
        
        
          was replaced, with increased cushion, and more blows were
        
        
          applied with no improvement of the measurements and with
        
        
          further crushing of the concrete.
        
        
          A second test pile was constructed and this time access
        
        
          tubes for CSL testing were cast in the pile. Concreting records
        
        
          showed potential problems near the toe and part way though the
        
        
          pour.  Observations suggested the concrete had started to set
        
        
          early, possibly due to the extreme temperatures.  CSL test
        
        
          results confirmed problems at the toe and between 15-20m
        
        
          below the pile top.  (Figure 4).
        
        
          Dynamic pile testing was also conducted and confirmed
        
        
          concrete problems.  Gauges were attached to the concrete
        
        
          through windows in the steel casing. Results suggested there
        
        
          was a significant defect  15-20m down the shaft.  The steel was
        
        
          also not contributing to the pile. Transfer of load by steel to
        
        
          concrete bond seemed unreliable.  (Figure 5).
        
        
          5
        
        
          PRODUCTION SOCKETED PILES
        
        
          As it was thought the cause of the concrete problems was
        
        
          known, and related to temperature and the behaviour of concrete
        
        
          additives, it was decided to proceed with production piles, but
        
        
          only at abutments, where repairs such as additional piles were
        
        
          possible.
        
        
          
            Figure 3 PDA measurements on steel
          
        
        
          
            Figure 1 - Pier foundation Layout
          
        
        
          
            Figure 2 - PDA measurements on concrete