 
          1243
        
        
          Technical Committee 202 /
        
        
          
            Comité technique 202
          
        
        
          remaining near or below 0.3. This behaviour was commonly
        
        
          observed elsewhere along the project..
        
        
          Figure 2 Ch 4+185m Deformation Ratio & Fill Height v Time
        
        
          The distribution of measured peak deformation ratio
        
        
          throughout areas of the project improved by PVD and surcharge
        
        
          is shown in Figures 3 (a), (b) & (c) for the mainline
        
        
          embankment south and north of the River Shannon plus
        
        
          Clonmacken Link respectively.
        
        
          In general peak deformation ratios south of the Shannon
        
        
          were kept below 0.6. Exceptions occurred at Ch 1+900 &
        
        
          2+850 m where the embankment was constructed adjacent to
        
        
          and within the original course of Ballinacurra Creek and
        
        
          temporary sheet piling had to be employed to maintain stability.
        
        
          Within the mainline north of the Shannon peak deformation
        
        
          ratios were typically below 0.5. Exceptional values in excess of
        
        
          1.0 occurred near Ch 7+550 m & 7+650 where local failure of
        
        
          an existing back drain behind the Shannon flood protection
        
        
          bund and instability in an area where the surface crust had been
        
        
          historically removed for brick manufacture. In both cases local
        
        
          instability occurred at relatively low embankment heights and
        
        
          was mitigated by culverting the drain and incorporation of
        
        
          geogrid reinforcement over short sections of the outer
        
        
          embankment slope. Other high ratios occurred near the
        
        
          locations of cross ditches.
        
        
          Along Clonmacken Link several values in excess of 1
        
        
          occurred associated with failures which are described in more
        
        
          detail below. Interestingly the occurrence of high deformation
        
        
          ratios is not particularly correlated to maximum embankment
        
        
          height nor to the inclusion of basal geosynthetic reinforcement
        
        
          within the embankment. Around 90% of all survey monitored
        
        
          sections demonstrated a deformation ratio of under 0.6.
        
        
          4.2
        
        
          
            Embankment Failures at Clonmacken Link
          
        
        
          During the period from June to September 2007 two significant
        
        
          failures occurred over 50m lengths of embankment (from Ch
        
        
          140 to 190 and from Ch 780 to 830m ) as filling extended their
        
        
          height to around 3 - 3.5m. Both failures occurred on the left
        
        
          (northern) side of the embankment and displaced a relatively
        
        
          shallow block of alluvium up to 2.5m deep at the toe outwards
        
        
          and closing a ditch constructed from 5 to 15m distant from the
        
        
          toe. In both cases the failure plane was restricted to the
        
        
          outermost section of embankment and did not pass through the
        
        
          basal reinforcement or the drainage blanket which appeared to
        
        
          function normally based on the nearest piezometer records.
        
        
          Forensic investigations of both failures revealed the
        
        
          following factors which had contributed to the instability:
        
        
          
        
        
          Accidental over steepening of side slopes to around 1:1.3 in
        
        
          lieu of the design slope of 1:2 (V:H);
        
        
          
        
        
          Presence of nearby ditches, especially drains cut skew or
        
        
          transverse to the embankment;
        
        
          Figures 3 (a), (b) & (c). Peak Deformation Ratio v Chainage,
        
        
          Mainline South, North & Clonmacken Link respectively.
        
        
          
        
        
          Poor quality fill (Moisture Condition Value 5 to 8 with
        
        
          significant organics) compounded by wet weather
        
        
          conditions (Ch 140 – 190 m only); and
        
        
          
        
        
          High filling rates around 1.5 to 3 m/week.
        
        
          Typical deformation ratio history for instrumented location
        
        
          at Ch 0+150 m is shown on Figure 4. The large incremental
        
        
          settlements > 0.1m observed in early to mid September 2007
        
        
          plus deformation ratio approaching 1.0 immediately prior to
        
        
          failure in mid September both validate the selection of design
        
        
          threshold values and were both reliable indicators of future
        
        
          instability. Regrettably the data was not passed quickly enough
        
        
          to engineers who could have acted to avert the failure by
        
        
          preventing further filling after 17 September 2007. The final
        
        
          filling rate of around 3m / week (1.3 metres in 3 days) could
        
        
          never be sustained at this site and resulted in failure.